So far so good if I dare say so. The freeze plug in question blew out twice under minimal pressure at the machine shop. Turns out the hole is 10 thousandths oversize. As for the coolant in the crankcase that's still a mystery. Neither head gasket was blown and the after pressure testing and magnafluxing the heads and block again we found no leaks or cracks. Turns out the break in oil is green and I wasn't aware of that. In all the excitement I may have overreacted and assumed the green color was coolant. Still doesn't explain the high level on the oil dipstick. Could it have been overfilled? Possible I suppose. A new gasket set is on order and we're preparing to reassemble and test again. I'm keeping my fingers crossed that it will be ok. From there the motor is being taken into another shop for Dyno-testing. I don;t want to have to do this again so that should reveal any issues and allow for fine tuning prior to it being reinstalled. I'm looking forward to putting this debocle behind me asap.
Bookmarks